罗金恒, 杨锋平, 马秋荣, 赵新伟, 魏进家, 王海涛. 新建大落差管道试压排水爆管原因分析[J]. 油气储运, 2011, 30(6): 441-444.
引用本文: 罗金恒, 杨锋平, 马秋荣, 赵新伟, 魏进家, 王海涛. 新建大落差管道试压排水爆管原因分析[J]. 油气储运, 2011, 30(6): 441-444.
Luo Jinheng, Yang Fengping, Ma Qiurong, . Reason analysis on pipe fracture in hydrotest during water draining for a newly-built pipeline with great fall[J]. Oil & Gas Storage and Transportation, 2011, 30(6): 441-444.
Citation: Luo Jinheng, Yang Fengping, Ma Qiurong, . Reason analysis on pipe fracture in hydrotest during water draining for a newly-built pipeline with great fall[J]. Oil & Gas Storage and Transportation, 2011, 30(6): 441-444.

新建大落差管道试压排水爆管原因分析

Reason analysis on pipe fracture in hydrotest during water draining for a newly-built pipeline with great fall

  • 摘要: 基于两次爆管的4个相似特征,分析了某大落差管道两次试压排水爆管原因:事故管道高程存在起伏,排水时管道高点聚集气体,排水后期,由于排水口径较小,试压头背压较大,在清管器推动下,气体压缩破裂,引起弥合水击,产生瞬时高压,击破钢管。根据水击增压公式的估算结果,弥合水击产生的瞬时高压可达41.6 MPa,大大超过该管道的承载极限。为验证该论断,在第三次试压排水中,增大排水口径以减小水击影响,同时在线监测爆管处附近的压力。此次试压排水顺利完成,并且在排水末期监测到峰值为1.75 MPa的典型水击压力信号,证明气体确实存在

     

    Abstract: Reason analysis on two-time pipe fractures in hydrotest during drainage for a great fall pipeline was made based on four similar characteristics in the fractures. This pipeline was laid along an elevated area, and air was accumulated at the high spot of pipeline when water drainage was conducted in hydrotest. In the later stage of drainage, the backpressure of pressure head was quite high due to the small size of drainage hole, the air was compressed to burst under the push of pig, and a bridge water hammer was formed to produce an instantaneous high pressure to break up the pipe. According to estimation results derived from the water hammer boost pressure formula, the instantaneous high pressure caused by the bridge water hammer could be up to 41.6 MPa, and this result greatly exceeded the ultimate load of the pipeline. To verify the above conclusion, the drainage outlet was expanded to reduce the impact of water hammer, and the on-line monitoring on the pressure near the fracture point was carried out in the third drainage of hydro test with a satisfactory result. And the typical water hammer pressure signal with the peak value as 1.75 MPa was detected in the end of drainage stage, which proved that the air did exist.

     

/

返回文章
返回