林永刚, 邓忠华, 薛延军, 王迪. 阿独乌鄯系统密闭输送运行风险分析及PID参数整定[J]. 油气储运, 2021, 40(10): 1194-1200. DOI: 10.6047/j.issn.1000-8241.2021.10.016
引用本文: 林永刚, 邓忠华, 薛延军, 王迪. 阿独乌鄯系统密闭输送运行风险分析及PID参数整定[J]. 油气储运, 2021, 40(10): 1194-1200. DOI: 10.6047/j.issn.1000-8241.2021.10.016
LIN Yonggang, DENG Zhonghua, XUE Yanjun, WANG Di. Operation risk analysis for custody transfer of A-Du-Wu-Shan system and the PID parameter setting[J]. Oil & Gas Storage and Transportation, 2021, 40(10): 1194-1200. DOI: 10.6047/j.issn.1000-8241.2021.10.016
Citation: LIN Yonggang, DENG Zhonghua, XUE Yanjun, WANG Di. Operation risk analysis for custody transfer of A-Du-Wu-Shan system and the PID parameter setting[J]. Oil & Gas Storage and Transportation, 2021, 40(10): 1194-1200. DOI: 10.6047/j.issn.1000-8241.2021.10.016

阿独乌鄯系统密闭输送运行风险分析及PID参数整定

Operation risk analysis for custody transfer of A-Du-Wu-Shan system and the PID parameter setting

  • 摘要: 针对阿独乌鄯系统异常工况下手动流程切换不及时、调节阀PID控制压力调节时间长等问题,对改造后的两种运行方式进行风险分析并制定风险防范措施,明确了调节阀PID控制的优越性。利用工程整定法重新整定了乌鲁木齐进站调节阀PID参数,通过调节阀压差测试与应急工况模拟,验证了调节阀PID控制的可靠性能与快速处置能力,并对PID控制效果的影响因素进行了分析。结果表明:乌鲁木齐站整定后的PID参数能够实现流程切换和应急工况下进站调节阀快速精准的自动控制,压力调节时间由780 s降至约75 s,且震荡较小。研究成果可为调节阀精准控制及异常工况处理提供指导,并为实现管道智能调控奠定理论基础。

     

    Abstract: Aiming at the problems of untimely manual flow path switching under abnormal working conditions and long time required for pressure regulation through the PID control of the regulating valves of A-Du-Wu-Shan system, risk analysis was carried out for the two operation modes after transformation, appropriate risk prevention measures were developed, and the superiority of PID control of the regulating valves was clarified. Thereby, the PID parameters of the regulating valves in Urumqi Station were reset with the engineering tuning method, the reliability and the rapid disposal ability of the PID control of the regulating valves were verified by differential pressure test and emergency condition simulation, and the influencing factors of the PID control effect were analyzed. The results show that, the reset PID parameters of Urumqi Station can achieve the fast and accurate automatic control of the inlet regulating valves under flow path switching and emergency conditions, and the pressure regulation time decreases from 780 seconds to about 75 seconds with small oscillation. Generally, the research results could provide guidance for the accurate control and abnormal condition treatment regulating valves, and lay a theoretical foundation for the realization of intelligent control of pipelines.

     

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