李东风, 宋建河, 王海东, 褚军. 秦京管道混输冀东原油优化运行分析[J]. 油气储运, 2006, 25(3): 17-22. DOI: 10.6047/j.issn.1000-8241.2006.03.005
引用本文: 李东风, 宋建河, 王海东, 褚军. 秦京管道混输冀东原油优化运行分析[J]. 油气储运, 2006, 25(3): 17-22. DOI: 10.6047/j.issn.1000-8241.2006.03.005
LI Dongfeng, SONG Jianhe, . Analysis On Optimization Operation of Qinhuangdao-Beijing Oil Pipeline in Way of Blended Transportation Jidong Crude[J]. Oil & Gas Storage and Transportation, 2006, 25(3): 17-22. DOI: 10.6047/j.issn.1000-8241.2006.03.005
Citation: LI Dongfeng, SONG Jianhe, . Analysis On Optimization Operation of Qinhuangdao-Beijing Oil Pipeline in Way of Blended Transportation Jidong Crude[J]. Oil & Gas Storage and Transportation, 2006, 25(3): 17-22. DOI: 10.6047/j.issn.1000-8241.2006.03.005

秦京管道混输冀东原油优化运行分析

Analysis On Optimization Operation of Qinhuangdao-Beijing Oil Pipeline in Way of Blended Transportation Jidong Crude

  • 摘要: 对秦京管道因混输冀东原油后秦皇岛-迁安管段输量下降16%, 造成输油设备与运行工况不相匹配, 出现节流损失大、能源浪费大的问题进行了分析。通过采取相应的技术改造措施, 制定了秦京管道混输后的近期和长期优化运行方案。该方案实施效果表明, 优化运行方案科学合理, 目的性明确, 管道运行安全经济。

     

    Abstract: The analysis on the mismatch between transportation equipments and operation condition, more throttling loss and power consumption in Qinhuangdao-Beijing Oil Pipeline is made. This problem comes from the Jidong Crude's blended transportation in this pipeline which results in 16% decrease in oil throughput in Qinhuangdao-Qian'an pipeline section. In allusion to this problem, the corresponding technical measures for short-term and long-term optimized operation programs are worked out.

     

/

返回文章
返回